ARM: pxa/cm-x300: fix V3020 RTC functionality
While in sleep mode the CS# and other V3020 RTC GPIOs must be driven
high, otherwise V3020 RTC fails to keep the right time in sleep mode.
Signed-off-by: Igor Grinberg <grinberg@compulab.co.il>
Cc: stable@kernel.org
Signed-off-by: Eric Miao <eric.y.miao@gmail.com>
diff --git a/arch/arm/mach-pxa/cm-x300.c b/arch/arm/mach-pxa/cm-x300.c
index b2248e7..8a03487 100644
--- a/arch/arm/mach-pxa/cm-x300.c
+++ b/arch/arm/mach-pxa/cm-x300.c
@@ -161,10 +161,10 @@
GPIO99_GPIO, /* Ethernet IRQ */
/* RTC GPIOs */
- GPIO95_GPIO, /* RTC CS */
- GPIO96_GPIO, /* RTC WR */
- GPIO97_GPIO, /* RTC RD */
- GPIO98_GPIO, /* RTC IO */
+ GPIO95_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC CS */
+ GPIO96_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC WR */
+ GPIO97_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC RD */
+ GPIO98_GPIO, /* RTC IO */
/* Standard I2C */
GPIO21_I2C_SCL,